Figure 5: RO Normalized Differential Pressure vs. Time.
Conclusion
The six-week on-site pilot study, conducted by Veolia Water Technologies at a coal-fired power plant was a success. Designed to validate RO technology for treating the commingled well water as a pre-concentration step to a thermal ZLD system, the pilot study demonstrated the following:
• Potassium permanganate was more effective in oxidizing feed water iron and manganese than sodium hypochlorite. In conjunction with downstream filtration, removal goals were achieved.
• The RO system was successful in maintaining 55 percent recovery at process conditions for 34 days, using a specialized scale inhibitor.
• The RO system operated with stable normalized permeate flow, normalized salt passage and normalized differential pressure without the need to clean the RO membranes.
• The RO system was operated at 60 percent recovery for three days, and although there was a slight drop in normalized permeate flow, the system did not operate long enough to draw conclusions on performance trends.
• The analytical results demonstrated that the treatment system achieved the treated water quality requirements. IWW
Editor’s note: The above article is a condensed version of the following paper, used with permission: Korpiel, J., Pudvay, M., and Hess, M., (2018). “Reverse Osmosis Treatment of Well Water Commingled with Flue Gas Desulfurization Wastewater at a Power Plant,” Proceedings of the 79th Annual International Water Conference, Scottsdale, Ariz., November 4-8, Document IWC 18-51.
About the Author: John Korpiel is a principal engineer with Veolia Water Technologies. He has 22 years of experience in industrial water and wastewater treatment, specializing in the process design, optimization, and troubleshooting of integrated membrane treatment systems. He has an M.S. degree in environmental engineering from the University of Pittsburgh and is a licensed professional engineer in Pennsylvania.